The bit of the plastic container that welded itself to the warming tray |
The replacement, filled and safely stashed in the much cooler tool tunnel |
I had been monitoring our online crew rostering facility with some interest in the lead up to Friday, as nobody had signed up to clean the loco. I was having visions of having to not only do all the pre-flight checks & the light up, but also having to clean Foremarke Hall as well. Ade, the driver for the day had also shared my concerns and
Gwendolyne at work with the Brasso (other brass cleaning products do exist) |
Tom using an alternative brass cleaning product. |
Ade oiling up Foremarke Hall |
Heading into the south headshunt whilst I operate the points. |
Breakfast came from the Flag & Whistle rather than the shovel on this occasion |
Lineside drainage gang at work between Gotherington & Bishops Cleeve. |
Gwendolyne, rather unimpressed that she is now a weather shield |
You wouldn't have guessed that it was hammering down five minutes earlier |
It makes sweeping around the footplate a bit of a challenge though. |
Gwendolyne earns some Brownie points. |
Go home light... you're drunk! |
3845's boiler being lifted (photo courtesy of Mike Solloway) |
3850's boiler being placed on 2874's chassis (photo courtesy of Mike Solloway) |
3850 swings round through 180 degrees (photo courtesy of Mike Solloway) |
2874's boiler swings round through 90 degrees (photo courtesy of Mike Solloway) |
Attaching chains to the chairs (photo courtesy of Peter Gutteridge) |
Up it comes (photo courtesy of Peter Gutteridge) |
3850... trapped! |
2874's rusted up vac cylinder (photo courtesy of Peter Gutteridge) |
The freed up end plates from 3850's (photo courtesy of Peter Gutteridge) |
David working on 2874's boiler, before starting on 3845's |
David (a different one) removing rust from the saddle area |
Track being dislodged... |
...and pulled free by the telehandler |
Popping out the sleepers |
The start of the sleeper stack. |
Rod was in the machine shop on Saturday, busy re-leading a number of GWR style fusible plugs for use on our locos. The plugs have an inner thread into which the lead is melted, of 1/2" W. Once the plug has been used once, it can be rebored to 9/16W and re-leaded. After the two uses, it is scrap and a new one has to be made. This process takes place during every boiler washout.
Removing surplus lead in the base of the plug |
Rod in the machine shop |
Gunmetal blanks for making the next batch. |
Trimming the lead core to a cone. |
The nearly finished product, almost ready to fit |
In fact, here are plenty that Rod made earlier, (scrap ones in the background.) |
Tweaking 35006's tender brakes. |
35006 enjoying the TLC |
And finally, one of Saturday's footplate crew managed to leave his hat behind at the end of the day. Helpfully, one of the many reprobates still present marked the inside of the hat with its owner's name for ease of identification.
Coo! We ain't half missed you on the blog. What an absolutely unrivalled 'whizz' of a blog! I am at a loss to recall when we were treated to such a wonderful potted collection of items. Great blog. Regards, Paul.
ReplyDeleteGood to see Rod still beavering away on the machines
ReplyDeleteDave Scott
Great to see a blog from the steam dept again
ReplyDeleteGreat blog again-welcome back! The item on water testing reminded me of a colleague whose early job on the railway included sending off water samples to I think, one of the major railway workshops on a weekly basis. Getting fed up with the same standard response, he decided to liven things up by sending off a sample of his own- so to speak! The reply was immediate-'This horse is fatally ill and must be put down immediately'.
ReplyDeleteExcellent and informative blog thank you
ReplyDelete