Anyway, stupid O'clock on Saturday morning arrived and I turned up at Toddington MPD to start cleaning 5542. Now remember she had only just arrived, I rather expected her to be pretty much shining like a new pin, in reality she had been used on a fire & drive course the day before and was now more than just a little grubby. Never mind, there was a good turn out of cleaners and we all selected something to clean and got cracking with it.
Andrew (Left) & Karl proudly show off their handiwork |
Students of Collett small prairies, would probably like to know just what detail changes have taken place on 5542 during her winter holiday down on the South Devon Railway. If you look closely, you will notice that she now has autocoach gear just under her front buffer beam which wasn't there before. If only we had three or four autocoaches to run with her. Something that came as a bit of a surprise to me was that she now has a tilting grate fitted. Clive Norton the fireman for the first shift today seemed to be pleased to find it there.
It's a bit late now to show it tilting, but somewhere in there is a tilting grate |
Emptying out the ash pit isn't usually the world's most interesting job, however Cliff and Ade set to the task and Cliff discovered that he wasn't alone in the pit.... in fact he was very much playing gooseberry to a pair of amorous interlopers who were in there with him.
Cliff and Ade emptying the pit of ash |
Toad of |
Now that 5542 was nicely spruced up ready for her meeting with the history books, there was time in hand before she set off, to repair to the Flag & Whistle for one of Val Hoskin's delicious full English breakfasts! Just as well really, as it turned out to be the last I'd eat for another 12 hours.
Well so far the weather wasn't behaving, but everything else was going according to plan. The allotted time came and wearing my nice shiny new hi-viz I set off to grab a few photos of the first departure from Toddington.
5542 stands at Toddington station, ready to depart |
Off she goes |
Well so far, so good, the plan was starting to come together. Having plenty of time before 5542 got down to Cheltenham and started coming back, I headed off back into the yard to see what wanted doing. As it turned out, both 2807 and Foremarke Hall both needed lighting up. Not having done a light up since passing out to do them sometime before Christmas, this seemed like a perfect opportunity to get some practice in and soon enough I was whizzing around the loco running through the safety checks before cleaning up the grate and getting a fire going, meanwhile, Chris Chewter was doing the same with 2807. As it turned out, the goal posts were running around all over the place. It was initially supposed to be a case of bringing her up to steam enough to check that after some work, the lubrication system was getting oil through to the front end, but that was changed to joining 2807 as double headed light engines on a fitness to run exam for 2807 up to Laverton and back. You can't abandon a loco when it's lit up, so both Chris & I spent much of the day from around 10am through to 4pm minding our engines and keeping them from blowing off. As a consequence, my plan to report on this blog of the historic return to Laverton by steam etc came to nothing. I shall have to refer you instead to excellent reports on the matter elsewhere, such as the Steaming to Broadway blog and of course the main GWSR website.
The best that I could manage from my vantage point on the footplate of Foremarke Hall was this shot of 5542 returning from Laverton to Cheltenham
5542 on first run from Laverton to Cheltenham |
Chris taking a break from getting 2807 into steam |
I suspect that they may have told me a porky pie as regards the sun!
Now remember that the locos were supposed to be off shed and down to Laverton together at 4pm. I had a bit over three quarters of glass of water and sat steady at about 220 PSI by about quarter to four. I'd been sat there for nearly 6 hours and kept her from blowing off in all that time. By and large I was feeling fairly pleased about it. The fire was a bit run down at this point, so I decided to fill up a few of the points where it was a little light and have her perfectly ready for setting off at four. No sooner than I had done that, than the news that we would now be leaving at twenty to five came along. Needless to say my water space was all used up and she was blowing off nicely by then.
I had been meaning over the last month to take a ride out to Laverton on the DMU to learn the route, but had always found other things to occupy my time on the railway, so I was keen if possible to grab a ride there and back on the footplate. Cliff & Adrian not only allowed me to join them on the run, but Cliff left me to do the firing, though in reality I don't recollect that I needed to shovel in any coal, just keep the fire spread out over the grate and bung in some water now and again when she was getting close up to the red line again.
2807 leads Foremarke Hall back to Toddington from Laverton Loop |
2807 heads off first, 5542 will follow her onto road 9, then we will head off down road 8 |
I had cause to be at Toddington again for a bit on Sunday morning too. As it was passing whilst I was sat in the mess coach, I grabbed a photo of 5542 heading off for Cheltenham. Andy Beale remarked to his crew as they went by 'Looks like we're going to be on the blog tomorrow chaps', so I'd best not disappoint them.
Andy Beale driving 5542 yesterday |
when having a project like this we should be watchful on the products that we use to prevent accidents..
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