Sunday marked the end of
the regular timetabled running season, all that is left now is the Santa/Mince
Pie specials and then the steam loco dept goes into hibernation until the
spring. Well ok, hibernation isn't quite
the right word, the locos won't be running, but the railway will be a hive of
activity with the locos undergoing winter maintenance and the numerous other projects
around the railway will continue unabated.
Sunday was also the last day of operation out of Winchcombe; henceforth
all engines will be prepped & disposed at Toddington again.
November is shaping up
to be the wettest on record, rather like most of the other months this year and
Sunday was of course the day after half a week's worth of the sort of prolonged
rain that had people building arks and rounding up two of every kind of
animal. Building an ark is quite a
challenge at the moment as most ash trees have succumbed to chalara fraxinea
and apart from the ducks, all sensible animals were hiding themselves out of
the rain. This intensity of precipitation
presented a number of issues; my usual route from the M5, the B4077 was badly
flooded, the inspection pit at Winchcombe was flooded and kept filling up from
leaks even when pumped out and finally, the sheet covering the wood store had
failed abysmally in its task of keeping the wood for lighting up dry. This last
detail was of particular importance to me as I had arranged to do another
assessed light up with Paul Richardson.
Last time round he had been concerned that I was taking quite a while to
explain everything that I was doing and so this time I elected to turn up half
an hour early and after signing on/reading the notices, checking the loco was
safe etc. I cleaned the grate which gave me something of a head start for when
Paul arrived. So that is exactly what I
did, and I was particularly pleased to note that today's service loco was the
8F, complete with its 'Happy Handle'. The
job is so much easier with a rocking grate!
Anyway, 6am arrived and I was ready.
Unfortunately Paul didn’t show up.
Kevin Hoskin did appear though and agreed that I should start the light
up procedure under his supervision, which we did. Paul appeared about quarter of an hour later,
it turns out that he hadn't been quite as foolhardy as me and had turned round
at the flood on the B4077 to try and find an alternative route rather than just
ploughing on through as I had done.
Anyway, the light up went pretty smoothly; the only foul-up was that I
lit the fire before re-installing the baffle plate. I have now made a note to myself to place it
on the driver’s side of the cab in future where I'll notice it, rather than
hide it behind me.
Since last week, the
existence of this blog has been officially announced to the entire steam loco
dept. It has had the desired
effect of attracting one article for inclusion written by somebody else other
than me (thanks Geof), hopefully more will follow. Now that it is public knowledge, I am now either actively
encouraged to take photos of people for inclusion on these pages..... Or more
usually people have now taken to avoiding me even more than before, especially
if I have a camera in my hand.
Coming in under the category of the less camera shy are:
Ian Butler, busy oiling up Foremarke Hall in readiness for the Elegant
Excursions dining train on Sunday lunch time.
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Ian Butler |
Ex-BR fireman Derek
Smith, who was busy getting Foremarke Hall into steam. I'm not completely sure that his hat is
standard BR issue!
|
Derek Smith |
Ben Evason was the guard
for the service train on Sunday, a bit of a busman's holiday as he is also a guard
on the big railway and as if that isn't enough he also passed out as a driver
on the GWSR earlier this year. At some
point during the day he quoted a rhyme to me relating the high esteem in which
drivers and guards hold each other in.
Sadly I can't remember exactly how it goes however suffice it to say
that it came under the heading of NSFW.
I'm also now in his bad books for omitting to switch on the steam heat
during one of the earlier runs of the day.
|
Ben Evason |
People less eager to be pictured, but who were captured on the digital
equivalent of film anyway included Paul Richardson, here preserving for
posterity with his own camera the last day's running from Winchcombe.
|
Paul Richardson and 45160 |
Chris Chewter was caught
with his hands in the sink of the mess coach under the supervision of George Forrest. Apparently you have to get passed out on all
aspects relating to domestic kettles before you get let loose with the 4'
8.5" variety. Marks will definitely
be deducted if you get it wrong and put coal in the tea pot and shovel tea bags
onto the grate, though there are some who would say that even decaffeinated tea
bags would probably burn better than the coal that we had in last week.
|
George Forrest & Chris Chewter |
The wooden patio set
used for tea breaks on the rare days that it wasn't raining had somehow found
its way into the wood store and was unceremoniously launched into the firebox of 45160.
|
The demise of the patio set |
An unexpected bonus was
the appearance of David Shepherd who owns Black Prince, which
until relatively recently was based on the GWSR.
|
David Shepherd |
David was here to take a few pictures of
Foremarke Hall for a painting that he has been commissioned to make. Here are a couple of photos of Black Prince
when she was based here, many would love to see her return again, including me.
|
Black Prince at Winchcombe |
|
Black Prince approaching Greet tunnel from Gotherington |
Andy Webber who was
fireman of the 8F on the afternoon shift has kindly provided me with this shot
of Phil Grange installing the new hose pipes at Toddington a few weeks ago. It's a bit odd that a couple of firemen were busy installing kit to put fires out with, perhaps they have got confused and think that they are the kind that arrive on big red engines with blue flashing lights rather than green engines with copper chimney caps.
|
Phil Grange |
Speaking of Andy Webber, here he is chatting with Dan Wigg at clocking off time at Toddington after a hard day on the footplate of 45160.
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Andy Webber chatting to Dan Wigg |
Finally, yours truly has
been working away this week, spending the first half of the week in Manchester
and arriving in Crewe today for the rest of the week. What on earth as this got to do with the
GWSR? Well the answer is that that Pete Waterman’s loco restoration workshop,
LNWR Heritage is at Crewe and I couldn’t pass up the opportunity to pop in and
see how the boiler for 4270 is coming along.
Even though the place was closed to visitors, they were very welcoming and more than happy to let me wander around and grab a few photos.
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The frames & cab of 4270 at Toddington |
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4270's boiler at Crewe |
The chap in the foreground was busy fabricating the boiler cladding. I asked when they thought it would be finished, without expecting an answer more informative than "when it's finished" only to be told that they were hoping to send it down to Toddington on Thursday the 6th of December.
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